Skip to content
KLUNK
KLUNK

2002 Dodge Stratus

The Verdict

59 Proceed with Caution

The 2002 Dodge Stratus has 174 owner complaints filed with NHTSA. The most reported issues are body (58 complaints) and engine (57 complaints). With a Klunk Score of 59/100, it earns a "Proceed with Caution" rating. If you're shopping for a Dodge Stratus, consider the 2005 model year which has 64% fewer complaints.

Safe Bet

The 2005 has 64% fewer complaints

View the 2005 Dodge Stratus dashboard →

59

Klunk Score: Proceed with Caution

About average for complaint volume. Research the specific issues before buying.

How is this calculated?

The Klunk Score ranks this vehicle year against all others in our database based on total owner complaints filed with NHTSA. 100 = fewest complaints (top tier), 0 = most complained-about. Scores above 60 are better than average; below 40 means more problems than most.

Get notified if a recall hits this car.

We email you when NHTSA issues a new recall on the 2002 Dodge Stratus. No spam, no marketing.

Under the Hood

Each number is a complaint. Darker = bigger problem.

YearBodyBrakesElectricalEngineTransmission
200010327365419
20017211305917
20025812295718
200339722176
20046110263710
200522511213
200626416234

By Category

Body
58
Engine
57
Electrical
29
Transmission
18
Brakes
12

By Severity

1
71
2
83
3
1
4
19

Worst Problems

Complaints

Electrical 1

TL* THE CONTACT OWNS A 2002 DODGE STRATUS. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 15V338000 (AIR BAGS) HOWEVER, THE PART TO DO THE REPAIR WAS UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE MANUFACTURER WAS NOTIFIED OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE. PARTS DISTRIBUTION DISCONNECT.

125mo ago
Electrical 2

TL* TAKATA RECALL. THE CONTACT OWNS A 2002 DODGE STRATUS. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 15V338000 (AIR BAGS) HOWEVER, THE PART NEEDED TO PERFORM THE REPAIR WAS NOT AVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE THE CONTACT HAD NOT EXPERIENCED A FAILURE. VIN TOOL CONFIRMS PARTS NOT AVAILABLE.

126mo ago
Body 2

CRACKS IN THE DASHBOARD. CAR DOESN'T SIT IN MUCH DIRECT SUNLIGHT. APPEARED OUT OF NOWHERE. I AM CONCERNED ABOUT SAFETY ISSUES REGARDING AIRBAGS. ALSO NOT AESTHETICALLY PLEASING ON OTHERWISE NICE INTERIOR. I DO NOT TAKE THIS VEHICLE ON BUMPY ROADS.

127mo ago
Electrical 1

TL* THE CONTACT OWNS A 2002 DODGE STRATUS. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 15V338000 (AIR BAGS) HOWEVER, THE PART TO DO THE RECALL REPAIR WAS UNAVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER HAD EXCEEDED A REASONABLE AMOUNT OF TIME FOR THE RECALL REPAIR. THE MANUFACTURER WAS NOT MADE AWARE OF THE ISSUE. THE CONTACT HAD NOT EXPERIENCED A FAILURE. THE VIN TOOL CONFIRMS PARTS NOT AVAILABLE.

130mo ago
Electrical 4

TL* THE CONTACT OWNS A 2002 DODGE STRATUS COUPE. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 15V338000 (AIR BAGS) AND STATED THAT THE PART WAS NOT AVAILABLE WITHIN A REASONABLE TIME FRAME TO SCHEDULE THE RECALL REPAIR. THE DEALER DID NOT GIVE A SPECIFIC DATE FOR WHEN THE PART WOULD BECOME AVAILABLE. THE MANUFACTURER COULD NOT PROVIDE AN ESTIMATED DATE FOR WHEN THE VEHICLE WOULD RECEIVE THE RECALL REPAIR. A MONTH AGO, WHILE DRIVING AN UNKNOWN RATE OF SPEED, THE CONTACT STRUCK A DEER AND THE AIR BAGS DID NOT DEPLOY. THE CONTACT SUSTAINED PAINS TO THE RIGHT LEG, RIGHT KNEE, AND FOOT. A POLICE REPORT WAS NOT FILED AND THE CONTACT DID NOT RECEIVE MEDICAL ATTENTION. THE VEHICLE WAS NOT INSPECTED TO DETERMINE WHY THE AIR BAGS DID NOT DEPLOY. THE MANUFACTURER AND THE DEALER WERE CONTACTED FOR SEVERAL MONTHS AND THE CONTACT WAS UNABLE TO DETERMINE WHEN THE RECALL REPAIR WOULD BE COMPLETED. THE FAILURE MILEAGE WAS UNKNOWN.

131mo ago
Body 1

TL* THE CONTACT OWNS A 2002 DODGE STRATUS. WHILE DRIVING 35 MPH, THE VEHICLE STALLED. THE CONTACT WAS ABLE TO RESTART THE VEHICLE. UPON FURTHER INSPECTION, THE CONTACT NOTICED THAT THE REAR DRIVER SIDE BALL JOINT FRACTURED FROM THE VEHICLE. THE VEHICLE WAS TOWED TO A DEALER WHO DIAGNOSED THAT THE BALL JOINT NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED; HOWEVER, THE FAILURE RECURRED OVER TIME WITH THE REMAINING THREE BALL JOINTS DETACHING FROM THE VEHICLE. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 186,000.

131mo ago
Electrical 2

TL* THE CONTACT OWNS A 2002 DODGE STRATUS. THE CONTACT RECEIVED NOTIFICATION OF NHTSA CAMPAIGN NUMBER: 15V338000 (AIR BAGS); HOWEVER, THE PART TO DO THE REPAIR WAS NOT AVAILABLE. THE CONTACT STATED THAT THE MANUFACTURER EXCEEDED A REASONABLE AMOUNT OF TIME TO PROVIDE THE PART TO DO THE REPAIR. THE CONTACT HAD NOT EXPERIENCED A FAILURE.

132mo ago
Engine 1

THE INTERNAL WATER PUMP FAILED. THIS CAUSED WATER TO LEAK INTO THE OIL PAN. THE WATER GOT HOT ENOUGH ON A 600 MILES TRIP FROM FLORIDA TO MISSISSIPPI THAT IT BOILED AND CAUSED THE OIL TO TURN INTO SLUDGE (MOLASSES LIKE CONSISTENCY). THIS CAUSED A LACK OF LUBRICATION OF THE DUAL CAMSHAFTS WHICH IN TURN BURNED UP. END RESULT WAS ENGINE FAILURE.

132mo ago
Body 4

MY CAR HAS A BAD NOISE AND POPPING SOUND IN THE FRONT END. I WAS TURNING OUT OF MY MOMS DRIVEWAY WHEN MY FRONT PASSENGER TIRE COLLAPSED IN .. MY UPPER BALL JOINT BROKE . AFTER MY CAR WAS JACKED UP MY LOWER A ARM AND BALL JOINT WAS BROKE .. I REPLACED EVERYTHING . A WEEK LATER THE DRIVER SIDE BALL JOINT HAD TO BE REPLACED . MY CAR STILL MAKES A AWEFUL SOUND LIKE SOMETHING IS ABOUT TO BRAKE . SHOULD I REPLACE EVERY PART IN THE FRONT . CAUSE IT DANGEROUS FOR MYSELF AND MY CHILD .

136mo ago
Body 1

MY DAUGHTER PULLED OUT OF MCDONALD'S TURNING RIGHT AND THE LEFT WHEEL COLLAPSED UNDER THE VEHICLE. THERE WAS NO ACCIDENT AND NO ONE WAS INJURED. I HAD IT TOWED TO OUR HOUSE. I HAVE READ ON LINE AND FOUND THAT IT IS A COMMON PROBLEM. *JS

138mo ago
Electrical 4

SPEAKER IN THE BACK CARGO AREA STARTED SMOKING AND CAUGHT FIRE AND STEREO SHORTED OUT. *TR

143mo ago
Electrical 1

TL* THE CONTACT OWNS A 2002 DODGE STRATUS. THE CONTACT STATED THAT WHILE MAKING A TURN, THERE WAS AN ABNORMAL NOISE COMING FROM THE STEERING WHEEL. IN ADDITION, THE CONTACT STATED THAT UPON STARTING THE VEHICLE, THE AIR BAG WARNING LIGHT ILLUMINATED. THE VEHICLE WAS NOT DIAGNOSED OR REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 78,000.

144mo ago
Body 1

TL* THE CONTACT OWNS A 2002 DODGE STRATUS. THE CONTACT STATED THAT WHILE DRIVING AND MAKING A TURN, THERE WAS AN ABNORMAL NOISE COMING FROM THE FRONT DRIVER SIDE OF THE VEHICLE. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHO DIAGNOSED THAT THE FRONT DRIVER SIDE LOWER CONTROL ARM AND BALL JOINT NEEDED TO BE REPLACED. THE VEHICLE WAS REPAIRED AND TWO WEEKS LATER THE CLICKING NOISE RECURRED. THE VEHICLE WAS TAKEN BACK TO AN INDEPENDENT MECHANIC, WHO DIAGNOSED THAT THE CONTROL ARM WAS CRACKED. THE CONTROL ARM AND BALL JOINT WAS REPLACED FOR A SECOND TIME AND TWO WEEKS LATER THE FAILURE RECURRED FOR A THIRD TIME. THE MANUFACTURER WAS NOTIFIED OF THE FAILURE. THE FAILURE MILEAGE WAS 191,300.

145mo ago
Electrical 2

TL* THE CONTACT OWNS A 2002 DODGE STRATUS. THE CONTACT STATED THAT THERE WAS AN ABNORMAL NOISE FROM THE DASHBOARD AS THE AIR BAG WARNING LIGHT ILLUMINATED. THE VEHICLE WAS TAKEN TO AN INDEPENDENT MECHANIC WHERE IT WAS DIAGNOSED THAT THE AIR BAG NEEDED TO BE REPLACED. IN ADDITION, THE HORN AND THE CRUISE CONTROL FAILED. THE VEHICLE WAS NOT REPAIRED. THE MANUFACTURER WAS MADE AWARE OF THE FAILURE. THE FAILURE MILEAGE WAS 65,000 AND THE CURRENT MILEAGE WAS 69,000. UPDATED 09/02/14*LJ

146mo ago
Engine 4

GRANDAUGHTER WAS RETURNING HOME FROM COLLEGE . VEHICLE SUDDENLY CAUGHT FIRE ON HIGHWAY BETWEEN MARBLE FALLS TEX AND BURNET TEXAS.. HER MOTHER WAS FOLLOWING IN ANOTHER CAR AND BARELY HAD TIME TO RESCUE SOME OF THE PERSONAL ITEMS BEFORE ENTIRE CAR WAS ENGULFED IN FLAMES. GRANDDAUGHTER BARELY ESCAPED THE VEHICLE WITHOUT INJURY. SHE WAS ABLE TO GET SEVERAL PICTURES OF THE VEHICLE FIRE ON HER CELL PHONE.. THE FIRE BEGIN EITHER UNDER THE HOOD OR UNDER THE FRONT OF THE CAR AND WAS COMPLETELY ENGULFED IN A MATTER OF MINUTES.. GRANDAUGHTER AND HER MOM WAS VERY DISTRAUGHT AND TERRIBLY UPSET UNTIL FIRE DEPT FROM BURNET ARRIVED ON THE SCENE . THEY WERE CALLED (911) BY A PASSING MOTORIST. THE BURNED OUT VEHICLE WAS HAULED IN TO BURNET TEXAS BY ADVANTAGE TOWING 512-756-7995. WE HAVE NEVER RECEIVED A RECALL FROM DODGE ABOUT THE POSSIBLE FIRE HAZARDS ON THIS VEHICLE. *TR

150mo ago
Electrical 1

I HAD SMELLED A BURNING SMELL IN MY CAR WHILE I DRIVE IT. MY HUSBAND HAD TRIED HIS BEST TO FIND WHERE THE SMELL IS COMING FROM. WE COULD NOT FIND IT AND NOW MY RADIO DOESN'T WORK, THE DOME LIGHT DON'T WORK AND THE LOCKS DON'T WORK. IN ORDER TO LOCK MY CAR I HAVE TO PUSH THE LOCKS DOWN. CAN YOU PLEASE HELP ME WITH WHAT COULD BE THE POSSIBILITY OF WHAT'S WRONG WITH MY CAR? I HAVEN'T BEEN DRIVING IT. *TR

151mo ago
Engine 1

NOTICED SLIGHT GEAR SLIPPAGE TRAVELLING 35-45MPH. ALL FLUIDS CHECKED, AT PROPER LEVELS. A WEEK LATER, ENGINE 'JERKED' WHEN COMING TO COMPLETE STOP, CHECK ENG LIGHT ILLUMINATED. PROGRESSIVELY WORSENED. ONCE ENGINE WARMED UP, STARTED HEARING A 'WHIRRING' NOISE FROM LOWER-MIDDLE AREA OF ENGINE. STOPPED @ LOCAL REPAIR SHOP, THEY CHECKED FLUIDS AND VAC HOSES, NOISE STOPPED, BUT NOTICED COOLANT IN RESERVOIR SIDE 3/4 FULL & BOILING, TEMP GAUGE ON DASH 'NORMAL'. NEXT DAY, WHILE COLD, I CHECKED COOLANT LEVEL IN RESERVOIR (LEFT SIDE) STILL FULL, (HADN'T FLOWED BACK THRU SYSTEM ONCE COOL). I ADDED WATER TO 'FILL LINE', CHECKED CONDITION OF PRESSURE CAP (LOOKED FINE), PLACED & TIGHTENED, STARTED ENGINE, LET RUN A FEW MINUTES, LOOSENED 'AIR BLEEDER' ON TOP OF COOLANT BLEEDER HSNG. THEN I SLOWLY SHIFTED THRU ALL GEARS, W/FOOT ON BRAKE, LET AIR BLEED TIL SOLID STREAM OF LIQUID AND SHUT CAR OFF. WAITED AN HOUR, STARTED UP AND DROVE. CK ENG LT= OFF. FINE FOR A FEW DAYS, SAME ISSUES STARTED UP AGAIN. LOUDER 'WHIRRING', LIKE A BELT OR BAND SLIPPED. IRRATIC SHIFTING, TRANS NEVER FAILED. RAN BOTH CODE TESTS ON DASHCLUSTER=NO DTCS. JAN 2014-DROVE TO DODGE DEALERSHIP: DISPOSITION: REPLACE MOPAR 41TE TRANS. MY LOST WAGES / LOSS OF VEH USE(DEC/JAN) + BURDEN OF A LOAN TO REPLACE THE TRANSMISSION = MORE THAN I PAID IN FULL TO BUY THE CAR BARELY 6 MONTHS AGO. UNFAIR TO CUSTOMERS: ONGOING COMPUTER AND PCM/TRANSMISSION FAILURE SINCE 1999. THE 'OOPS' TECH SPEC-CORRECT TRANS FLUID ATF+4 HOW MANY DAMAGED & FAILED TRANSMISSIONS? REFUSED TO HONOR POWERTRAIN WARRANTY!! AND CONTINUED PLACING. SHAME ON ALL OF THE CORPORATE EXECUTIVES & ENGINEERS THAT GOT RICH FROM ROBBING THE CONSUMERS. YOU WERE 'SUCCESSFUL FAILURES' MOPAR, CHRYSLER-DODGE-DAIMER-IACOCCA, ETC. 90+ TSBS, NO RECALLS. CLASS ACTIONS DISMISSED! TIME FOR THE CONSUMERS TO PREVAIL. TIME FOR A CALIFORNIA CLASS ACTION!! *TR

152mo ago
Electrical 2

I GOT IN MY CAR TO DRIVE HOME AND AS SOON AS I STARTED THE CAR AND TURNED THE WHEEL JUST A LITTLE, I HEAR A POPPING SOUND COMING FROM THE STEERING WHEEL. THE LIGHT ON THE DASHBOARD CAME ON STATING "AIR BAG". I HAVE ALREADY HAD PROBLEMS WITH THE BALL JOINTS I HAD TO REPLACE MYSELF AND OTHER ISSUES WITH THIS CAR. NOW I HAVE A FAULTY AIR BAG THAT IS MAKING NOISE EVERY TIME I TURN THE WHEEL. I ALSO FOUND OUT I HAVE NO HORN. IT DOES NOT WORK SINCE THE AIR BAG IS FAULTY. I AM NOT PROTECTED WITH AN AIR BAG AND CAN NOT DEFEND MYSELF WITH MY CAR HORN...I NEED HELP! *TR

158mo ago
Brakes 1

TL* THE CONTACT OWNS A 2002 DODGE STRATUS. THE CONTACT STATED THAT WHILE DRIVING 20 MPH, THE REAR DRIVER SIDE BACKING PLATE FRACTURED AND CAUSED THE WHEELS TO SEIZE. THE VEHICLE TAKEN TO AN INDEPENDENT MECHANIC. THE TECHNICIAN VERIFIED THE FAILURE AND STATED THAT THE BACKING PLATE, CALIPER, BRACKET, AND PARKING BRAKE SHOES NEEDED TO BE REPLACED. THE MANUFACTURER WAS NOT MADE AWARE OF THE FAILURE. THE VEHICLE WAS REPAIRED. THE FAILURE AND CURRENT MILEAGE WAS 50,000. *TR

161mo ago
Electrical 2

TL* THE CONTACT OWNS A 2002 DODGE STRATUS. THE CONTACT STATED WHILE DRIVING 30 MPH THE AIR BAG LIGHT ILLUMINATED AND BEGAN MAKING A BEEPING NOISE. APPROXIMATELY 60 SECONDS LATER THE PASSENGER SIDE AIR BAG DEPLOYED IN THE DIRECTION OF THE WINDSHIELD. THE WINDSHIELD WAS CRACKED AS WELL AS DAMAGING THE DASH BOARD. THE VEHICLE WAS TAKEN TO A DEALER FOR DIAGNOSIS AND AN ENGINEER WAS DISPATCHED TO INSPECT IT. OVER A MONTH LATER THE CONTACT RECEIVED A LETTER FROM THE MANUFACTURER STATING THEY DID NOT FEEL THE FAILURE WAS DUE TO A MANUFACTURER DEFECT AND WOULD OFFER NO ASSISTANCE. THE FAILURE AND CURRENT MILEAGE WAS 140,000.

166mo ago

174 total

1/ 9
Report a Klunk